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Ts101 #1695
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Update ShowStartupWarnings.cpp Update OLED.hpp Update stm32f1xx_hal_msp.c Update Setup.cpp Update Power.cpp Update Pins.h Update configuration.h Power Muxing Working dual input Voltage handler Scan mode required for differing injected channels Inject both dc readings Update configuration.h Update configuration.h Use htim4 for adc control on TS101 Refactor htim names Add ADC_TRIGGER Speed up BB I2C a lil Update configuration.h Update startup_stm32f103t8ux.S Update configuration.h Add LIS2DH clone LIS2DH gains another clone Create tooling to allow mapping accelerometers onto different buses Update startup_stm32f103t8ux.S Ensure PD IRQ is pulled up
Update ShowStartupWarnings.cpp Update OLED.hpp Update stm32f1xx_hal_msp.c Update Setup.cpp Update Power.cpp Update Pins.h Update configuration.h Power Muxing Working dual input Voltage handler Scan mode required for differing injected channels Inject both dc readings Update configuration.h Update configuration.h Use htim4 for adc control on TS101 Refactor htim names Add ADC_TRIGGER Speed up BB I2C a lil Update configuration.h Update startup_stm32f103t8ux.S Update configuration.h Add LIS2DH clone LIS2DH gains another clone Create tooling to allow mapping accelerometers onto different buses Update startup_stm32f103t8ux.S Ensure PD IRQ is pulled up Allow toggle which button enters PD debug
Going to have to figure out why USB-PD isnt working another day, out of time for today. |
I can confirm much of the functionality works. Here are two USB PD captures of me plugging the iron into a 65 W UGREEN power supply and into a power bank: These are Sigrok format files, decodable with PulseView 0.5, and have been captured by a ChromiumOS Twinkie type device. EDIT: The previous set of captures I posted was corrupted on my end due to instrument issues, I've reuploaded different ones. |
Thanks for the captures. Have done a bunch of ideas but nothing seems to change it so far. |
Update stm32f1xx_it.c
Update BSP.cpp
Update push.yml
I built the latest version and gave it a quick test. It appears usable for soldering with a PD power source I have, however there are a few issues:
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Thanks for the test
That is going to vary display-to-display, different OLED's start at different thresholds
I'll try and look into this.
Hmm, yep I can probably shift this around, I dont hear it here on my unit (checked with spectrogram app on phone).
This is still entirely out of scope, as to clear the GRAM we need support for the larger buffers etc. And I would rather ship something than hold this for weeks/months until I have time to deal with OLED stuff. |
Hello @L1cardo / hello @VioletEternity, regarding the noise, if I may suggest, could you please check using a phone/mobile app the actual frequency of the sound? It's kind of strange the sound occurs near temperature setpoint, when the power consumption is actually the smallest during heat session. In short, the power train (actual pulse that controls the power FET) is a 10kHz (or 5kHz?) signal, 50% duty cycle. Let's say it's 10kHz. This 10kHz square signal is gated / modulated by a gate pulse with variable duty-cycle (the width of the gate pulse is under the dynamic control of IronOS and this is the way the average output power is controlled). The frequency of this gate pulse is about 100Hz if I recall correctly. At setpoint, the width of the gate pulse has the smallest value (duty-cycle of only few percent) while at full power, the power gate duty-cycle goes up, near to "100%" (more like 95%). However, it never reaches 100% as we need a small window of time (few ms), when no power is injected into the tip, and during this window, the temperature (and other) measurements are performed. Now, if the sound frequency is around 10kHz is one thing / if it's a clean 100Hz frequency is another thing / if it's a 10kHz sound modulated by a 100Hz envelope (probably a microphone + oscilloscope would be required to conclude this) would be yet, another thing. I am tempted to suspect that the last case is true. Most likely the sound is always there (10kHz) during heat session, but the human ear starts perceiving it only when the sound is significantly modulated. This would explain why it seems to appear near setpoint. It also would be good to know if on TS101, Miniware preserved (or not) the AC coupling between the command signal and the gate pin of the power FET (as used with TS100). In the "Addendum: Outline of functional blocks" (see @VioletEternity post #1420 (comment)) I could not notice any capacitors in the gate / power area. It could be that they are placed elsewhere on the PCB or maybe on TS101 they went with a simple, direct DC coupling, in which case that 10kHz power train is no longer needed and the power could be controlled directly by the current gate / modulation pulse, in which case the high pitch sound would probably go away. The alternative (and this would be easy to test) would be to increase the frequency of the power train from 10kHz to 20kHz (by lowering the timer 3 period), in which case most of the people (old guys like me for sure) would not hear a damn thing :-). I could not test it on TS101 as I don't have one, but on TS100 the 20kHz power train seems to work just fine. |
As for the suggested test change, this should be done in IronOS/source/Core/BSP/Miniware/Setup.cpp at line 270: |
Hello @L1cardo, you dropped that picture without a word. I initially thought it's timebased / oscilloscope like frame. Now, I'm thinking that most likely what you dropped is in fact a histogram (FFT). Is that what you posted? |
That's ok @L1cardo. It looks like a FFT histogram to me (on X axis we have the frequency and on Y axis the amplitude of the harmonic at a specific frequency). The issue is FFT analysis on "piezo" soundwaves generated by square electrical signals is tricky. As a square signal is basically a superposition of an infinity of harmonics of various amplitudes, you don't get clean results, and most often multiple harmonics out of which you don't know which one matches the excitation frequency. For such cases, it is preferable to just analyze the recorded sound (as a plain time-based sequence) and get the main frequency / see the signal modulation (if any) from there. |
Nevertheless @L1cardo, you could try the suggested changes in the firmware. If you still hear the high-pitch sound afterwards, it means you either have an exceptionally good sense of hearing or the sound could actually come from elsewhere (like the PD power supply used to power the iron). In that case, switching to a plain DC power supply (powering the TS101 via its DC barrel) would make any difference? |
The TS101 is direct tip drive, so there is no ac coupling capacitor anymore. Instead the 50% duty cycle is replaced by the pwm value instead. https://github.com/Ralim/IronOS/pull/1695/files#diff-1eddd86b1c0ecb235a3774a6edd96ebaf75b1d1ab570bdd58629aa93a092c387R138 Other Irons have not been audible at this frequency, but we can definitely shift it down. Going higher seems to run into issues with something not fully switching in very quick tests I did. If someone wants to do testing, I would suggest adjusting the prescaler here: https://github.com/Ralim/IronOS/pull/1695/files#diff-089752d1b62731302cc1ebf92ed076fbeea024af8f5a8818c5b61de467c88f5aR310 |
Hello @Ralim, that's good as it simplifies a bit the timers stuff. At a first glance, in the new, TS101 dedicated code (thank you for the links!) the htimTip timer, at a prescaler of 2690 (in fast PWM) would lead to a timer tick rate of about 2.97kHz (8MHz / (2690 + 1)). Then considering the constant period set for 255, this would lead to a htimTip cycle frequency of about 11Hz. There is no way this would lead to the reported high pitch noise (7-15kHz), disregarding the pulse width / duty-cycle, dynamically set at runtime. |
Forgot to update since I changed the period
Realised I forgot to update the prescaler when I increased the period; can you try latest build artefacts 🙇🏼 |
@sandmanRO For the TS101 I suspect its mostly happening as we scale back duty cycle on the tip control PWM, as the PWM gets shorter the harmonics will get worse too. (as well as I forgot to update the prescaler when I bumped the max from 100 to 255 which I just pushed). |
Oh man, there are so many changes since last time I was looking over the code. Brand new code all over the place. I'm petrified that you managed to write so much code in such a short time. I feel like I should apologize for the change suggestions I made, as they no longer have anything to do with the new code. |
And one more thing, after I flashed IronOS, I can notice that the heating up speed is significantly slower than the stock firmware. |
Can I have some more details on what build this was, and what power supply was being used ? |
@L1cardo, if the current is the same in full power, there is little reason the tip would heat up slower. This is a physical fact. What it could be different is the way the PID drives the average power near the temperature setpoint. For that, to exclude the subjective sense of timing, why don't you do this: have the setpoint set at 300 Celsius. Then using a chronometer / stopwatch you measure how long it would take to heat up the tip from the room temperature to 270 degrees and 300 (setpoint) degrees respectively. You would have to repeat the experiment on both cases, when running IronOS and when running Miniware firmware. |
Miniware firmware: 15.0s->270°C,17.4s->300°C |
Ok, we are getting somewhere. Have you noticed at what temperature the IronOS starts to drop from full power to less than full power? |
I mean, from the data you have collected, from room to 270 the IronOS "falls behind" by about 3 seconds, then, on the last 30 degrees, the delay almost doubles, so this backs up that this is related to the way the PID drives the temperature to setpoint. You can lead the temperature aggressively, and most likely risk to overshot, or drive the temperature in a clean, asymptotic ramp to setpoint. It's a matter of choice. |
Yep that looks exactly like conservative tuning vs aggressive tuning. I think honestly all Irons need abit of a "tune up" to to speak after I cleaned up tuning to handle S60's tiny ass tip. Buttt hold me to improving the tune before release 👀 |
How about providing an option to switch between conservative tuning and aggressive tuning? |
Certainly an option, best if you open a new issue to track it so it doesnt get lost 😓
Yep it was merged in a little before TS101 |
I follow the discussion |
Tracking Adding support for TS101.
Using info from #1420
Todo:
Out of scope: