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ERIAY
(j.l
3 445k D5L5450 b
DEVELOPMENT AND CONSTRUCTION OF
A MOLYBDENUM TEST STAND
CENTRAL RESEARCH LIBRARY
DOCUMENT COLLECTION
LIBRARY LOAN COPY
DO NOT TRANSFER TO ANOTHER PERSON
If you wish someone else to see this
document, send in name with document
and the library will arrange a loan
OAK RIDGE NATIONAL LABORATORY
OPERATED BY UNION CARBIDE CORPORATION e FOR THE U.S. ATOMIC ENERGY COMMISSION
Printed in the United States of America. Available from
National Technical Information Service
U.S. Department of Commerce
5285 Port Royal Road, Springfield, Virginia 22151
Price: Printed Copy $5.45; Microfiche $0.95
This report was prepared as an account of work sponsored by the United
States Government. Neither the United States nor the United States Atomic
Energy Commission, nor any of their employees, nor any of their contractors,
subcontractors, or their employees, makes any warranty, express or implied, or
assumes any legal liability or responsibility for the accuracy, completeness or
usefulness of any information, apparatus, product or process disclosed, or
represents that its use would not infringe privately owned rights.
(m
ORNL-4874
UC-80 — General Reactor Technology
Contract No. W-7405-eng-26
METALS AND CERAMICS DIVISION
DEVELOPMENT AND CONSTRUCTION OF A MOLYBDENUM TEST STAND
Compiled by
J. R. DiStefano A.J. Moorhead
Principal Contributors
N. C. Cole R. E. McDonald
J. R. DiStefano A. J. Moorhead
December 1972
OAK RIDGE NATIONAL LABORATQORY
¢ Qak Ridge, Tennessee 37830
operated by
UNION CARBIDE CORPORATION
for the
U.S. ATOMIC ENERGY COMMISSION
LOCKHEED MARTIN ENERGY RESEARCH LIBRARIES
AR
3 Y456 0515450 &
—_—
—_—
CONTENTS
A TaCt L L o e e e 1
Introduction . ........ ... .. i i e 1
Design of Test Stand . . ... ... e 3
Fabrication Development . ... ......... e e 6
Primary Fabrication of Molybdenum Components . . . ... ... ... ... ... .. . . . .. ... ... . ..... 6
Tubing Development . ... .. . ... . ... . ... ... e 10
Joining Development .. .. e 14
Welding . ... 14
Brazing . ..o e 27
Mechanical Couplings . . ... ... o 34
CONS U I ON L .. e e e e e 38
Mockup Construction . .. ... ... 38
Fabrication and Prefit of Components . ... ... .. . . . .. 41
Fabrication of Subassemblies . . . ... ... . . 42
Interconnection of Subassemblies .. ... ... .. 43
Acknowledgments . . ... e 43
Appendix A — Specifications for Purchase of Molybdenum Tubing . ... ... ... ... ... ... ... ...... 44
Appendix B — Electron Beam Welding Parameters for Tube-to-Header Joints ... .................. 57
Appendix C — Parameters for Welding of Butt Joints in Molybdenum Tubing Using
an Orbiting-Arc Weld Head . ... ... . . 58
iii
[ {
DEVELOPMENT AND CONSTRUCTION OF A MOLYBDENUM TEST STAND
Compiled by
J. R. DiStefano A. J. Moorhead
Principal Contributors
Cole R. E. McDonald
N. C. ‘
J. R. DiStefano A.J. Moorhead
ABSTRACT
The discovery of a process that uses liquid bismuth at 500 to 700°C to remove protactinium and
fission products from the molten salt fuel of a breeder reactor led to a search for suitable containment
materials. Although several other refractory metals or graphite may be suitable, molybdenum appears
most promising. Therefore low-carbon, low-oxygen molybdenum prepared by arc casting was chosen
as the structural material for a reductive-extraction test stand that would be representative of typical
equipment. We recognized that the use of molybdenum as a structural material would require
unorthodox assembly procedures and impose stringent limitations on the system design. However, this
material apparently possesses the best combination of properties such as fabricability, and oxidation
and corrosion resistance. Final design was determined after the development of appropriate fabrication
and joining techniques. ' '
Procedures were developed for the production of closed-end molybdenum half sections by back
extrusion. Parts that were generally free from cracks and had high-quality surfaces were produced by
the use of ZrOj,-coated plungers and dies and extrusion blank preheat temperatures of 1600 to
1700°C. In cooperation with a commercial vendor, we found that molybdenum tubing with improved
ductility could be produced by careful removal of contamination introduced during tubing
fabrication. :
Complex components were fabricated by welding, using either the gas tungsten-arc or
electron-beam process. Welding studies centered on three major types of joint: tube-to-tube, tube-to
header, and header-to-header. Two of the most important factors found to minimize weld hot cracking
were stress relieving and.preheating of components prior to welding. Mechanical bonding techniques
were developed to join small-diameter tubing to back-extruded end sections. Experiments carried out
at 250°C in an argon atmosphere produced helium leak-tight joints. Brazing filler metals were
developed that are reasonably corrosion resistant to bismuth and molten salt up to 700°C. Techniques
involving induction or resistance heating were developed to braze the several types of joints used in the
test stand. .
The Molten-Salt Reactor Program was terminated before construction of the test stand was
completed, but an unjoined mockup using molybdenum components was assembled, and detailed
assembly procedures were worked out. All of the techniques required for final assembly were
demonstrated.
INTRODUCTION
A key feature in the conceptual design of the single-fluid molten-salt breeder reactor is the connecting
chemical processing plant to continuously remove protactinium and fission products from the fuel salt (Fig.
1). Protactinium, the intermediate element in the breeding chain between thorium and ?°?U, has a
significant neutron capture cross section and must be kept out of the core to obtain a good breeding ratio.
Rare-earth fission products are also neutron poisons and must likewise be removed for good breeding. In
1968 the chemical feasibility of a process that uses liquid bismuth containing dissolved lithium and thorium
as reductants to extract protactinium and rare earths from fuel salt containing both uranium and thorium
was demonstrated.! A simplified flowsheet based on this process is shown in Fig, 2.
One of the requirements for the development of the reductive-extraction process is identifying materials
that are compatible with both molten fluoride salts and bismuth containing reductants. Hastelloy N
1. M. E. Whatley and L. E. McNeese, Molten-Salt Reactor Program Semiannu. Progr. Rep. Feb. 29, 1968, ORNL-4254,
pp. 248-51.
PRIMARY
SALT PUMP
I
— |
—
PURIFIED
SALT
GRAPHITE
MODERATOR
REACTOR l
HEAT
EXCHANGER T
566°C =
ORNL - DWG 68-{185ER
SECONDARY
NaBF,—NaF SALT PUMP
COOLANT SALT ’
CHEMICAL
PROCESSING
PLANT
FUEL SALT
T .
LiF ~BeF, - ThF, - UF,
——— STEAM GENERATOR
)
/)
. TURBO-
GENERATOR
STEAM
Fig. 1. Single-fluid, two-region molten-salt breeder reactor.
FUEL SALT
ORNL-DWG 71-9004
RECONSTITUTION
Ufg
URANIUM
REMOVAL
REACTOR | S—
EXCESS U
'FOR SALE
UFg
PROTACTINIUM RARE EARTH
—(--
REMOVAL REMOVAL
FISSION PRODUCTS
TO WASTE
Fig. 2. Simplified flowsheet for processing the fuel in a molten-salt breeder reactor.
(Ni—7% Cr—16% Mo—5% Fe) is a likely material of construction for the reactor because it has excellent
compatibility with molten salts at 500 to 700°C. However, nickel has appreciable solubility in bismuth at
these temperatures and, therefore, is unsuitable for those portions of a processing plant that have to contain
liquid bismuth. Other commonly used construction materials such as iron- or cobalt-base alloys have lower
solubilities in bismuth but rapidly mass-transfer under conditions involving a temperature gradient. Several
refractory metals (tantalum, molybdenum, tungsten, rhenium)Z:3 and graphite4 appear promising, but each
has limitations with respect to either fabricability, oxidation resistance, or compatibility with bismuth and
salt.
When it was proposed to build a reductive-extraction column that would be representative of typical
equipment and in which distribution coefficients for various elements could be checked and engineering
performance data determined, molybdenum was chosen as the material of construction. We felt that it
possessed the best combination of properties required for the processing application, namely, corrosion and
oxidation resistance, availability, and fabricability. However, no system this complex had ever been
constructed of molybdenum, and we foresaw many difficult fabrication problems that would have to be
solved.
Molybdenum is a particularly structure-sensitive material; that is, its mechanical properties are known
to vary widely, depending upon how it has been metallurgitally processed. The ductile-brittle transition
temperature of molybdenum varies from below room temperature to 200—300°C, depending both up.on
strain rate and the microstructure of the metal. Maximum ductility is provided in the stress-relieved
fine-grained condition, and recrystaltization and grain growth are known to reduce fracture stress and
ductility. Interstitial impurities such as oxygen and carbon often segregate at grain boundaries, and this can
result in a decrease in grain-boundary mobility which also favors premature fracture and low ductility.>
However, recent advances in vacuum-melting practices have led to the production of material with
improved and more reproducible metallurgical properties. The arc-melted low-carbon, low-oxygen grade of
molybdenum, available commercially, affords relatively good control of grain size and interstitial impurity
level. Nevertheless, the use of molybdenum as a structural material requires highly unorthodox assembly
procedures and imposes stringent limitations on system design from the standpoint of geometry and
rigidity.
DESIGN OF TEST STAND
The principal molybdenum components of the test stand are the column, disengaging pots, bismuth and
salt feed pots, and connectinig piping (Fig. 3). The column consists of a |'-in.-OD Raschig-ring-packed
central column for contacting countercurrent streams of bismuth-lithium and molten fluoride salt. Enlarged
end sections (37%-in.-OD pots) are provided for deentrainment and separation of the exit stream from the
entering stream. The fluids flow countercurrently through the column because of their difference in
density, and they are returned to their respective feed pots by an argon gas-lift system. Flow rates of the
fluids are controlled by orifices located in the bottom of the 37%-in.-OD feed pots (Fig. 4). The orifices are
removable, and different sizes may be used to allow a range of flow rates compatible with the limited head
available in the feed pots. The feed pots contain internal baffles and Raschig rings (Fig. 4) to deentrain
2. H. Shimotake, N. R, Stalica, and J. C. Hesson, “Corrosion of Refractory Metals by Liquid Bismuth, Tin, and Lead
at 1000°C,” Trans. Amer. Nucl. Soc. 10, 141—42 (June 1967).
3. J. W. Siefert and A. L. Lower, Jr., “Evaluation of Tantalum, Molybdenum, and Beryllium for Liquid Bismuth
Service,” Corrosion 17(10) 475t—-478t (October 1961). ‘
4. Molten Salt Reactor Program Semiagnnu. Progr. Rep, Feb. 29, 1972, ORNL-4782.
5. Molybdenum Metal, Climax Molybdenum Co., 1960, pp. 78—82.
ORNL-DWG 72-5404
(3% in. OD x Bin. LONG)
FEED POTS
SALT
FLOW METERING ORIFICE ]
6 |
UPPER Bi—SALT
T DISENGAGING POT
=== (3% in. OD x18in. LONG)
T TsALT
L ‘ ARGON —» fi
/
.- EXTRACTION COLUMN
(1%5in.OD x 5ft LONG)
{saLr
( LOWER Bi—-SALT
DISENGAGING POT
(3%in. OD x 16:in. LONG)
SALT
Bi
ARGON —» =
U INTERFACE POSITION INDICATOR
Fig. 3. Schematic of molybdenum reduction-extraction test stand. Overall, 11/2 ft in diameter and 17 ft high.
liquid from the argon in the gas lift and damp flow surges. The feed pots contain an access port for
sampling and for adding thorium or lithium to the system. More cdmplete details on the design of the test
stand have been reported elsewhere.6-7 '
One major problem in the fabrication of complex molybdenum equipment is its lack of ductility after
recrystallization. For optimum fabricability, it should be subjected to at least a 50% reduction in area after
recrystallization and then given a stress-relief treatment. Although we felt that the 37%-in.-OD pots could be
produced by machining from bar stock, material in this size range would have poor as-machined properties
because it would have received bnly a limited amount of working. The capacity of available metal-working
equipment was limited to using starting or blank material only slightly larger than the required finished
pots. We chose instead to fabricate these components by back extrusion, a process in which a cylinder with
a closed end can be produced by hot working in the range 1200 to 1700°C.
-Although molybdenum can be welded, the process generally results in very large grains in both the
fusion and heat-affected zones. Molybdenum welds are very brittle at room temperature and have a
tendency to hot-crack. We thought that our best chances for successfully welding molybdenum would be
6. E. L. Nicholson, Conceptual Design and Development Program for the Molybdenum Reductive Extraction
Equipment Test Stand, ORNL-CF-71-7-2 (July 1971).
7. W. F. Schaffer, Jr., E. L. Nicholson, and L. E. McNeese, Quality Assurance Program Plan for the Molybdenum
Reductive Extraction Equipment Test Stand — Job No. 12172, ORNL-CF-73-1-45 (February 1973).
ORNL-DWG 7i-3745R2
COUNTERBGRE
2-4mils GREATER THAN
TUBE DIAM FOR
RAZE CLEARANCE—-| |—~_L
=
'/gin. 1/4 in H 2
' \ A
T QS % A\
TYPICAL DESIGN FOR
l/l/’//
P Ll
NIY 77777
Ygin. TUBE-TO-HEADER
TYPICAL EB WELD
DESIGN FOR |.0.020in.
ROLL-BONDING (TYP)
N 7,
TS TN BT TR
Z
/
rA
AND BACK BRAZING
T
LTSS T LI OIS LTSI TTLLLL,
&7
XIS
DESIGN FOR
EB WELD
VENT TUBE END
DETAIL
OUTLET
Fig. 4. Feed pot for molybdenum chemical processing loop.
with the electron-beam process, which minimizes contamination effects, heat-affected-zone problems, and
abnormal grain growth. However, electron-beam welding is not applicable for joining lengths of tubing
together or for joining the tubing to a pot where the tube passes completely through the end section. A
technique using the gas tungsten-arc welding process with an orbiting electrode was developed to make the
tube-to-tube butt welds, and a mechanical joining technique (roll bonding) was developed to make the
latter joints. In addition, reinforcement of all welded or roll-bonded joints by brazing served to strengthen
the joint as well as to add a barrier to fluid leakage if a crack developed. To utilize brazing, however,
required the development of a filler metal that would both be corrosion resistant to bismuth and salt and
have a melting temperature below 1200°C, the maximum temperature that we felt could be tolerated
before the molybdenum would become overly embrittled as a result of recrystallization and grain growth.
The development work undertaken was concomitant with design of the test stand, and there was a
definite interrelation between the two functions. The final loop design represented a compromise between
engineering requirements and progress made in the development of fabrication and joining procedures for
molybdenum.
FABRICATION DEVELOPMENT
Primary Fabrication of Molybdenum Components
R. E. McDonald
The choice of molybdenum as the construction material for the test stand presented several fabrication
problems. It was originally suggested that the pots and the large-diameter heavy-wall tubing be machined
from bar stock. However, our experience was that bar stock more than 1% to 2 in. in diameter had poor
mechanical properties. Most available mechanical properties data comes from thin sheet or small-diameter
rod which has been heavily worked, and we felt that an end cap machined from 4-in.-diam bar would be
weak and crack-prone.
Fabrication development started before the test-stand design was completed. One method considered in
making the pots was by forging heavy plate to form end caps and then welding them to heavy-wall extruded
pipe. We had previously developed techniques to fabricate heavy-wall thngsten pipe, and 4-in.-diam by %
in. wall by 50-in.-long sections had been made.® Molybdenum pipe could readily be produced using the
same techniques. The forged end caps would then be welded or brazed to the large pipe body, producing
the pot, and pots made by this technique would have good mechanical properties because of the mechanical
working necessary to shape them. Available equipment aided us in the choice of back extrusion for
producing the end caps and forward extrusion for producing heavy-wall tubing. The Metals and Ceramics
Division at ORNL has available a horizontal extrusion press with an extensive tooling inventory. Three-, 4-,
5.6-, and 7-in.-diam containers with stems were on hand. The water-nitrogen accumulator system was
capable of 1300 tons on the 4-in. stem, and an induction billet heater, 50 kW at 3000 cycles, was capable of
“heating 4-in.-diam, 10-in.-long billets to 2200°C in 45 min. '
The first attempt to produce an end cap by back extrusion was made using a 4-in.-ID container with a
Zr0,-coated split die having provisions for integral bosses, a solid die backer, and a 3-in.-diam stem with a
3-in.-diam ZrO;-coated tool-steel plunger attached. This is shown schematically in Fig. 5. A 3.950-in.-diam
molybdenum blank was heated to 1300°C in the induction heater under an argon atmosphere, transferred
to the container, and quickly pushed with the plunger. The blank neatly filled the die and flowed back over
the coated plunger, producing a 4-in.-OD product. The tooling was conventionally cleared from the
container, the die parted, and the plunger extracted. Several back extrusions were made to determine the
optimum temperature, boss configuration, and skirt lengths. Back extrusions were successfully made at
1200, 1300, 1400, and 1500°C, and the maximum skirt length we obtained was 4 in. at 1500°C.
During this phase of development, however, cracks were noted in the hemispherical portion and the
skirt ends. Although it was first suspected that they occurred during back extrusion, we noted that fine
cracks had been generated on the faces of the blank during machining, and we felt they could have been
transferred to the product.
In an effort to understand and eliminate this cracking problem, a blank was cut lengthwise into two
sections, and a '4-in. square grid network of grooves was machined into each half. The grid of one half was
filled with small-diameter tantalum wires, and the two halves were pinned together. The blank was heated
to 1650°C and back-extruded. The halves of the extrusion were easily parted, and Fig. 6 shows the flow
pattern of the molybdenum during extrusion. The flow pattern shows that the cylindrical extrusion blank
was first pushed forward, filling the die cavities to form the bosses. After it bottomed out against the solid
die backer, it flowed backward over the coated plunger to form the skirt. As the free surface of the skirt
flows backward between the plunger and the die body, it is essentially undeformed. Therefore, if fine
8. R. E. McDonald and G. A. Reimann, Floating-Mandrel Extrusion of Tungsten and Tungsten-Alloy Tubing,
ORNL-4210.
4 ]
ORNL - DWG 70-3877A
DIE BACKER PLUNGER
DIE HOLDER
¢ BLANK i
‘ 3-in. STEM
SLEEVE LINER
CONTAINER SLEEVE
Fig. 5. Tooling used in capsule fabrication by back extrusion.
Y-108581
Fig. 6. Flow pattern in a molybdenum back extrusion revealed by a network of tantalum wires installed in half of the
original blank.
cracks exist on the back edge of the starting blank, then cracks in the skirt edge will occur. To minimize
this type of cracking, the back edge of the starting blank was radiused and highly polished. At this point,
our machining procedure was modified to require that all blanks be chemically etched and dye-penetrant-
inspected after machining. Molybdenum, like tungsten, has a tendency of smearing over cracks during
machining or grinding, and unless etched, it is difficult if not impossible to detect fine cracks. If cracks were
detected, very fine grindin'g removed them prior to acceptance. This change in procedure noticeably
reduced cracking in the back-extruded product.
While demonstrating that end caps could be made reliably, we noted that fairly long lengths of skirt
were extruded back over the plunger. We then decided it would be feasible to back-extrude two halves to
make a pot. This approach would require one girth weld instead of the two required to attach the end caps
to an intermediate section of pipe, and it would also eliminate the need to extrude 3%-in.-OD, %-in.-wall
pipe.
In order to back-extrude the end cap with a long cylindrical section, we thought that it would be
necessary either to do it in several steps or to raise the preheat temperature of the blank. However, this led
to further complications, We found that the ZrO, coating on the plunger stayed intact for only one or two
pushes before it had to be recoated because the inner surface of the product was adversely affected. Also,
the increase in the preheat temperature to 1650°C caused galling and tearing of the outer surface of the
extrusion because of a reaction of the molybdenum with the steel container liner (Fig. 6). The lubricant
used by ORNL for all extrusions of molybdenum, molybdenum alloys, tungsten, and tungsten alloys is
what we term a base-metal oxide lubricant. At the hot working temperature of these metals and alloys a
liquid oxide forms which is an excellent lubricant (covered by USAEC patent 3,350,907). However, the
residence time of the back extrusion in the container is long when compared with that of a conventional
forward extrusion, and the liquid oxide breaks down as a lubricant as the temperature of the steel
approaches its melting point. We had observed that the surfaces of the extrusion that were insulated from
the steel by the plasma-sprayed ZrO, were not tearing (Fig. 6); therefore the tooling was changed so that
molybdenum was in contact only with ZrQ,-coated surfaces during extrusion. To do this the 5.6-in.-ID
container was used, in which a 5.6-in.-OD, 4-in.-1D, 9-in.-fong split die was inserted. The entire inner surface
of the split die was plasma-sprayed with ZrQ,. At this point, the end design of the pot was also changed
from a multiple-bossed hemispherical head to a large single-boss flat head as shown in Fig. 7. Three
8-in.-long back extrusions were made at preheat temperatures of 1600 to 1700°C with a stem load of up to
800 tons. When the length requirement of the half sections for the lower disengaging pot was increased to
9Y,s in., a new [2-in.-long die was made. Three long blanks were then back-extruded at 1600 to 1700°C
with stem loads up to 800 tons. These extrusions exhibited good outer and inner surfaces, and skirt
cracking did not exceed an inch in length. A typical back extrusion after machining is shown in Fig. 8.
We thus showed that by using existing equipment — the horizontal extrusion press — half sections for
the bismuth, salt, and the upper and lower disengaging pots could be made by back extrusion. A total of 12
back extrusions were produced for use in constructing the molybdenum test stand, and data concerning
these products are summarized in Table 1.
The second problem, the production of the large-diameter heavy-wall tubing for the packed column,
was solved using techniques developed under the High Temperature Materials and Tungsten Programs at
ORNL. About 6 ft of 1.16-in.-OD, 0.080-in.-wall tubing was required. For this, we used a 4-in.-OD,
l1-in.-ID, 7-in.-long billet, which was heated to 1600°C and extruded over a ZrQ,-coated mandrel at a
reduction ratio of 29:1. A second extrusion produced a tube 11% ft in length that was concentric within
0.007 in. tolerance in radius and with excellent outer and inner surfaces. The process used was the ORNL
1]
107985
™
.l
Fig. 7. Zirconium oxide-coated back-extrusion tooling with molybdenum starting blank and as-extruded pot half
section.
V111890
Fig. 8. Example of molybdenum back-extruded half section after machining.
10
Table 1. Molybdenum half sections back-extruded
for the molybdenum test stand
Extrusion Internal
Part E::i:éleorn temperature length Results
O (in.)
Feed Pot 1197 1600 4 No cracks
IFeed pot 1250 1600 "4 End cracks, 3.5 in. usable
Feed pot 1257 1600 4.5 End cracks, 3.5 in. usable
Feed pot 1259 1600 4.5 End cracks, 4 in. usable
Spare 1251 1600 4 End cracks, 3.5 in. usable,
, surface cracks on top
Spare 1256 1600 4 Surface cracks on top
Lower disengaging 1258 1600 8 No cracks
Lower disengaging 1260 1600 8 No cracks
Spare 1261 1600 8.5 Cracksin wall
Upper disengaging 1286 [700 9 No cracks
Upper disengaging 1290 1700 11 End cracks, 9.5 in. usable
Spare 1288 1700 9 Reextruded, crack in wall
floating mandrel technique, which is described in another report,” with the lubrication provided by
molybdenum oxide.
Even though a scale-up of the test stand would be required in construction of an actual chemical
processing facility, we feel that we have demonstrated primary fabrication techniques for molybdenum that
would be épplicable to containers up to 12 in. in diameter and 36 in. long. Fabrication of larger-sized
components would require the adaptation of other fabrication techniques, such as ring rolling or power
spinning, or the development of new techniques.
Tubing Development
J. R. DiStefano
Four sizes of molybdenum tubing were required, and these were obtained commercially, as listed in
Table 2. All of the material was purchased according to the following specifications:
Specification No.
(see Appendix A) Title
MET-RM-B208 Tentative Specification for Seamless, Arc-Cast Mo Tubing for High Temperature Service
MET-NDT-3 : Tentative Specification for Ultrasonic Inspection of Metal Piping and Tubing
MET-NDTH4 Tentative Methods for Liquid Penetrant Inspection '
Initial investigation of three heats of this tubing revealed differences in microstructure, hardness, and
response to heat treatment, but little difference in interstitial concentration (Table 3). Inspection of the
inside of the tubes revealed surfaces which were rough or pitted. Metallographic examination of the
as-received Y -in-OD tubing showed it was partially recrystallized. Heating to 925°C for 1 hr resulted in
complete recrystallization. However, both the ;-in.- and %;-in.-OD tubing were received in a cold-worked
condition. Heat treating to 925°C did not alter the hardness or microstructure of the %;-in. tubing, but the
'/,-in. tubing softened and was almost completely recrystallized. Since the interstitial element concentra-
tions in the different heats were essentially the same, we can assume that the surprisingly low
9. R.E.McDonald and C. F. Leitten, Jr., *“*Production of Refractory Metal Tube Shells by Extrusion and Flow-Turning
Techniques,” pp. 85-92 in Refractory Metals and Alloys IfI; Applied Aspects, vol. 30, ed. by Robert 1. Jaffee (Proceedings
of the Third Technical Conference, AIME}, Gordon and Breach Science Publishers, New York, 1966.
)
ay
11
Table 2. Molybdenum tubing for chemical processing loop
Tubing size
No. of e L. Stress relief by Source
oD Wall heats Identification manufacturer Vendor Manufacturer
(in.) (in.)
A 0.020 1 CPM-1 1 hr, 870°C TECO? Superior Tube?
% 0.025 3 CPM-2 1 hr, 870°C TECO Superior Tube
CPM-6 None TECO TECO
CPM-8 1 hr, 870°C TECO TECO
A 0.030 2 CPM-3 1 hr, 870°C TECO Superior Tube
CPM-8 1 hr, 870°C TECO TECO
% 0.080 1 CPM-5 1 hr, 870°C TECO TECO
9Thermo Electron Corp., Woburn, Mass.
bSuperior Tube Co., Norristown, Pa.
Table 3. Hardness, microstructure, and chemical analysis of molybdenum tubing
as a function of heat treatment
Size of
tubiflg Condition DP};?EC;IE)%SS 2) Microstructure Concentration (ppm)
(OD in.) Oxygen Carbon
l/4 As received? 237 Cold worked 69 80
A 1 hr at 800°C 258 Cold worked
Ya 1 hrat 925°C 250 Cold worked
% As received® 200 Partially recrystallized (10—15%) 69 50
% 1 hr at 800°C 243 Partially recrystallized
A 1 hrat 925°C 168 ' Completely recrystallized
i, _ As received? 242 Cold worked 69 40
YA 1 hr at 700°C 255 Cold worked
A 1 hr at 800°C 243 Cold worked.
A 1 hr at 900°C 236 Very slightly recrystallized
A 1 hrat 925°C 206 Almost completely recrystallized (90%)
4The tubing was stress relieved for 1 hr at 870° C before delivery.
recrystallization temperatures for the ¥-in.-'and '%,-in.-OD tubing were the result of working prior to
heat treating.
" To evaluate the ductility of the tubing, we devised a somewhat qualitative test in which a 0.5-in.-long
sample was impact-flattened a predetermined amount at different temperatures using the equipment shown
in Fig. 9. The load was applied by a 2300-g weight dropped a distance of 6 cm. To obtain a quantitative
measure of deformation, we divided the displacement (original ring diameter minus the minor axis diameter
of the tested specimen) by the original diameter of the ring. The results of some of these tests are given in
Table 4. The as-received "4-in.-OD tubing was “ductile” (no cracks) at room temperature, while we had to
heat samples of the %-in.-OD tubing to 150—250°C and the %, -in.-OD tubing to 300°C before they became
ductile.
The behavior of the Y;-in.-OD tubing was traced to a brittle layer on its inside surface, as indicated in
Table 5. Removal of 0.004 in. from the inside diameter (0.002 in. from the wall thickness) resulted in
lowering the temperature at which acceptable ductility was observed from 300 to 125°C; when 0.006 in.
12
Table 4. Ductility of as-received molybdenum tubing as a
function of deformation temperature
Stress relieved 1 hr at 870°C
of . Deformation Temperature .
tubing dlsp!acement/ tube ©0) Observation
(OD in) diameter (%)
1/4 8 25 Cracked where I} in tension
1/4 8 100 Cracked where ID in tension
A 3 200 Cracked where ID in tension
A 4 25 Cracked where ID in tension
-1/4 4 100 Cracked where ID in tension
A 4 150 Cracked where ID in tension
A 4 175 Cracked where ID in tension
A 4 200 Cracked where ID in tension
l/4 4 250 Cracked where ID in tension
Y 4 300 No cracks
3/3 6.5 25 Fractured into four pieces
% 6.5 100 Cracked in three places
% 6.5 150 Cracked in three places
3/8 6.5 250 ‘No cracks
3/8 3.25 25 Fractured into four pieces
3/8 3.25 100 Cracked in four places
3/8 3.25 150 No cracks
3/8 3.25 175 No cracks
3/8 3.25 200 No cracks
1/2 10 25 No cracks
Table 5. Mechanical behavior of 1/‘;-in.-OD tubing
from the inner surface
_as a function of removing incremental layers
Material
Deformation
removed displacement/tube Tem;zerature Observation
from diameter (%) co
ID (in.)
0.002 4 25 Hairline crack
0.002 4 125 Hairline crack
0.004 4 25 Hairline cracks
0.004 4 125 No cracks
0.006 4 25 No cracks
0.006 4 125 No cracks
0.008 4 25 No cracks
0.008 4 125 No cracks
0.010 4 25 No cracks
0.010 4 125
No cracks
@
A
13
DIAL ORNL-DWG 71-8693
INDICATOR
/ IMPACT
LOAD
STRAIN
7] INCREMENT .
SPUN GLASW?? o Yfifi\/ o
é{ INSULATION 77 Ry ), *=ARGON
MANUAL VARIAC g ? §
CONTROL b
\ b CLAMSHELL
? ! FURNACE
ZONE
CONTROLLED,
BY
TC-I {
\ T g }‘g-spmmsu
\\ é
/ 7=
/
Z
ZONE /
CONTRQLLED, /
&2 TC-2=2 % §
\ N LAVITE
7 "z INSULATION
‘ ELEVATING MECHANISM
Fig. 9. Schematic of equipment used to impact-test samples of molybdenum tubing.
was removed from the inside diameter, the material was ductile at room temperature. Chemical analysis
indicated that material from near the inside surface contained higher oxygen and carbon concentrations
compared with the bulk sample analyses (140 and 120 ppm, respectively, compared with 69 and 80 ppm).
We suspected that contamination of the tubing occurred during fabrication and that it was not removed
during subsequent cleaning or heat treating operations.
Removing material from the inside of the %-in.-OD tubing also improved its room-temperature
ductility, but its as-received microstructure (partially recrystallized as compared with the cold-worked
fine-grained % -in.-OD tubing) led us to believe that the fabrication schedule used in its production might
also be responsible for its lack of ductility. Consultation with the manufacturer!® led to the following
changes in our specifications:
1. Starting tube shell shall have an average grain size of ASTM No. 6. No grain shall be larger than
ASTM No. 3. . ‘
2. Starting size of tube shell to produce %-in. OD X 0.025-in. wall product shall be 1.125-in. OD by
0.250-in. wall or 1.125-in. OD X 0.187 in. wall. In either case, no more than two intermediate anneals shall
be used and the temperature shall be no higher than 815°C.
10. Thermo Electron Corp., Woburn, Mass.
14
3. Prior to the final stress relief, material shall be cleaned in an alkaline solution. The inside surface
shall then be mechanically cleaned by wire brushing and then pickled to remove 0.001 to 0.002 in. from
the wall. ]
4. Final stress relief shall be 1 hr at 800°C in dry hydrogen or vacuum (<5 X 107% torr).
A quantity of %-in.-OD tubing was purchased according to these modified specifications and was found
to be ductile at room temperature as measured by our flattening test. The ',-in.-OD tubing that was already
on hand was acid etched to remove approximately 0.005 in. from its inside diameter, and selected samples
were found to be ductile. It should be noted that, although the as-received “contaminated” tubing was not
ductile in the impact flattening test, it could be bent at room temperature without fracturing. Some
samples were bent up to 90° without evidence of cracks. The rate of bending was found to be important,
but the data were not quantitated.
Welding studies indicated that a preweld stress-relief heat treatment for 1 hr at 875 to 900°C was
desirable to minimize weld cracking; however, samples of '4-in.-OD material (CPM-3) became embrittled
when heated-to 925°C, and one heat (CPM-6) became embrittled when heated to 860°C. Tubing selected
for loop construction was heat treated for | hr at 900°C in vacuum after all bends had been made. In this
way, we took advantage of the as-received ductility of the material for bending and still satisfied the
requirements for a preweld heat treatment. ‘
JOINING DEVELOPMENT -
Welding
A.J. Moorhead
Material selection and preparation. Molybdenum has several characteristics that make it difficult to
fabricate into complex structures by welding. It has a tendency to (1) undergo hot-cracking, (2) develop
porosity in the weld fusion zone, and (3) undergo abnormal grain growth. In addition, it has a
ductile-to-brittle transition temperature in large-grained microstructures (such as occur in the heat-affected
or fusion zones of a weld) well above room temperature, which can easily cause fracture at ambient
temperature. This latter characteristic makes handling of welded components, such as during subsequent
assembly steps, quite difficult. Consideration was given in the selection of the base material and in the
design and fabrication phases of the program to ways to overcome or at least minimize these characteristics.
The selection of arc-cast molybdenum with low impurity element levels was significant to the welding
development portion of the program. Low impurity levels are very desirable for this metal (especially O, N, and
C) since small amounts of these elements have been shown to have adverse effects on the ductile-brittle tran-
sition temperature and weldability of arc-cast molybdenum.?1—1!3 Oxygen is especially detrimental, as it
forms low-melting eutectic films with molybdenmfi, and the presence of these films at grain boundaries can
cause hot-cracking in welds. Molybdenum produced by powder metallurgy techniques was not considered for
the test stand because welds in commercially available materials of this type have repeatedly been found to
contain large amounts of porosity.!? Therefore, the selection of low-carbon, low-oxygen arc-cast base
material helped to minimize two of the detrimental factors in welding molybdenum, namely, hot-cracking
- and porosity formation. Great care was also taken in all subsequent operations to ensure that these
11. T. Perry, H. S. Spacil, and . Wulff, “Effect of Oxygen on Welding and Brazing Molybdenum,” Welding J. 33(9),
442-5—448-5 (1954),
12. W. N. Platte, “Influence of Oxygen on Soundness and Ductility of Molybdenum Welds,” Welding J. 35(8),
369-s—381-s (1956).
13. W. N. Platte, “Lffects of Nitrogen on the Soundness and Ductility of Welds in Molybdenum,” Welding J. 36(6),
301-5—306-s (1957).
14. N.E. Weare and R. E. Monroe, Welding and Brazing of Molybdenum, DMIC Report 108, p. 3 (March 1959).
L )]
15
elements were not introduced into weldments by surface contamination or by an impure welding
atmosphere. _
In order to ensure that the welds were not adversely affected by surface contamination, all components
were cleaned using the portion shown below of a complex cleaning procedure attributed to. Ryan by
[0
Thompson: 13
1. Degrease with acetone.
2. Immerse for 5 min in a 65—80°C solution of 10 wt % sodium hydroxide, 5 wt % potassium
permanganate, and 85 wt % distilled water.
3. Rinse in flowing tap water, brushing to remove smut.
4. Immerse for 5—10 min in a room-temperature solution of 15 vol % sulfuric acid (95—97 % H,S0,), 15
vol % hydrochloric acid (37—38% HCI), 70 vol % distilled water, plus 6—10 wt % chromium trioxide
(CI’Og).
5. Rinse in tap water,
6. Rinse in distilled water.
7. Dry with hot air.
Although we did not find any correlation (as far as leak-tight welds were concerned) with the time
between cleaning and welding, when parts had been excessively handled after the initial cleaning, we did
take the precaution of repeating steps | and 4—7 of the procedure just prior to welding.
After chemical cleaning, all parts used were given a vacuum stress-relief treatment for 60 min at 875 to
900°C at a pressure of 5 X 107° mm Hg or less. In our preliminary work, we found that a stress-relief heat
treatment had a major effect on the weldability of the various forms of molybdenum. For example, one
half of a length of ¥%-in.-OD, 0.025-in.-wall tubing was cleaned as previously described and then stress
relieved in vacuum for 60 min at 875°C. The other half of the tube was chemically cleaned only. In a series
of bead-on-tube “field” welds on these two pieces by the orbiting gas tungsten-arc process, we found that
the welds on the cleaned and stress-relieved tube were crack-free, while those on the “cleaned only” tube
had extensive center-line cracking. Similar results occurred on other sizes of tubing and on back-extruded
half sections. We tried several other stressrelief temperatures to determine the lowest temperature that
would produce the desired improvement in weldability and at the same time have the least effect on
base-metal ductility due to recrystallization. A temperature of 875 to 900°C was apparently optimum from
a weldability standpoint for these components, and it had little effect on the base-metal microstructure, as
shown by Fig. 10. The combination of the chemical and thermal treatments left the components with
surfaces that were lighter gray in color than in the as-received condition, and there was no noticeable
grain-boundary attack by the etchant..
Welding procedure development. Procedures were developed for welding three major joint types for the
test stand, two of which are illustrated in Fig. 4. A “tube-to-header” type of joint was required in seven
locations in which a line terminated in the end of a back-extruded half section. A joint which we refer to as
a “cylindrical girth” joint was welded to attach pairs of half sections together to form the four-fvessels or
pots. Many welds of the “tube-to-tube’ type were required to attach various lines to stubs projeéilting from
the pots or to one of the six tees. Each of these joint types will be discussed separately below.
15. E. G. Thompson, “Welding of Reactive and Refractory Metals,” Welding Research Council Bulletin 85, p. 7
(February 1963). :
16
V107759 ¥107763 Y-107758
(a)) (b)) (c))
10. Effect of heat treatment (in vacuum) on the microstructure of -in.-OD, 0.030-in.-wall molybdenum tubing.
Etchant: 50 vol % H30,-50 vol % NH4OH. (@) As received, DPH 241; (b) 60 min at 900°C, DPH 236 (¢) 60 min at
925°C, DPH 206
Tube-to-header joint. There are seven major tube-to-header joints in the test stand. Four join
0.875-in.-OD, 0.080-in.-wall tubing (which is machined to 0.050-in. wall in the joint area) to the feed pots;
two attach 1.125-in.-OD, 0.060-in.-wall, 7.25-in.long stubs of the packed column to the disengaging pots:
and the seventh attaches a 5.25-in.-long machined tube (with a %-in.-diam section at the weld) to the upper
disengaging pot. There are also other miscellaneous joints of this type in the stand; for example, it was used
in attaching the weirs to the horizontal baffle plates shown in Fig. 11.
To facilitate making this type of weld between the massive bosses on the extruded half sections and the
relatively thin-walled tube, a groove or trepan was machined inside the pot around the hole to produce a
corner-flange joint, as previously illustrated in Fig. 4. This design provides a good heat balance between the
two components and excellent mechanical support for the weld. Its major drawbacks are that it is relatively
inacce:
ible for welding or nondestructive examination. The use of the electron-beam process overcomes
the accessibility problem for welding, and has the added benefit that it minimizes abnormal grain growth in
the fusion zone because it is a process with a high energy density and a low total energy input. Because this
type of joint is difficult to inspect by radiography or ultrasound, we relied on close parameter control,
fluorescent dye penetrant inspection, and/or helium leak detection as our quality assurance techniques
for these welds.
17
¥-117087
Fig. 11. Weirs electron-beam welded (at arrowheads) (o one of the baffle plates shown installed in the upper half of
the bismuth feed pot.
Procedures were developed for electron-beam welding tube-to-header joints in tube sizes of 'y, %, Vs
Uy, and 1% in. outside diameter. The parameters for welding all of these sizes of tubing are given in
Appendix B, and an example of these two welds
s shown in Fig. 12. The electron-beam welder used is of
the high-voltage, low-current type (150 kV, 0.040 A max) with a chamber 36 in. wide, 23 in. deep, and 24
in. high. In our preliminary welds, in which flat plates simulated the vessel ends, we made welds both by the
conventional method of rotating the work under the beam and by using u simple system for manually
% in. in diameter) on the workpiece. Although we made acceptable
rotating the beam in a circle (up to
welds using both techniques, we had greater difficulties in making reproducible welds with the
rotating-beam technique: so all subsequent prototy pe welds were made by rotating the joint rather than the
beam. This latter technique was
somewhat complicated for the two vent tube joints, which were located
away from the center line of the pot, as seen in Fig. 13. However, this was compensated for by a simple
diam
fixture with cross slides for centering the weld under the beam. A close-up of a 0.375-ir
tube-to-header weld is shown in Fig. 14, and a photomicrograph of a helium leak-tight weld joining a
1.125-in.-0D, 0.060-in.-wall tube to a back-extruded molybdenum header is shown in Fig.
18
Pio70 103077
¥-111689
Fig. 12. Back-extruded half section with two tube-to-header welds made by the electron-beam process.
Fig. 13. Off-centered vent tube weld (arrow) made by welding a “washer” to the tube and then welding the washer to
alip in the feed pot bottom.
19
A
Fig. 15. Cross section through a weld joining a 1.125-in.-OD tube to a half section. Etchant: 20 vol % Hy05-10 vol %
H,504 (96% H2504)~70 vol % H,0. 29X
~~Yszin.
| Y%in.
Fig. 16. Joint design used for connecting back-extruded half sections by the gas tungsten-arc proce:
of % in. was typically used